Pan Am Flight 845

Pan Am Flight 845

Boeing 747-100 similar to the accident aircraft
Accident summary
Date July 30, 1971
Type Pilot error
Site San Francisco International Airport, San Mateo County, California, USA
Passengers 199
Crew 19
Injuries 29 (10 serious)
Fatalities 0
Survivors 218 (all)
Aircraft type Boeing 747-121
Operator Pan Am
Tail number N747PA
Flight origin Los Angeles, CA
Stopover San Francisco International Airport
Destination Tokyo, Japan

Pan Am Flight 845 was a Boeing 747-121, registration N747PA, operating as a scheduled international passenger flight between Los Angeles, CA and Tokyo, with an intermediate stop at San Francisco International Airport (ICAO: KSFO).[1] On July 30, 1971, at 15:29 PDT, while taking off from San Francisco bound for Tokyo, the aircraft struck Approach Lighting System structures located past the end of the runway, seriously injuring two passengers and sustaining significant damage. The crew continued the takeoff, flying out over the ocean and circling while dumping fuel, eventually returning for a landing in San Francisco. After coming to a stop, the crew ordered an emergency evacuation, during which 27 passengers were injured while exiting the aircraft, with eight of them suffering serious back injuries.[1][2][3] The accident was investigated by the NTSB, which determined the probable cause was the pilot's use of incorrect takeoff reference speeds. The NTSB also found various procedural failures in the dissemination and retrieval of flight safety information, which contributed to the accident.[1]

Contents

Aircraft

The Boeing 747-121, registration N747PA, manufacturing serial number 19639, was manufactured on January 29, 1970 and delivered to Pan Am on October 3, 1970, as the first 747 "Jumbo" airliner in its fleet, and the third 747 off Boeing's production line. It had logged 2,900 hours of operation at the time of the accident.[1][4]

Accident history

Flight 845's crew had planned and calculated their takeoff for runway 28L, but discovered only after pushback that this runway had been closed hours earlier for maintenance,[6] and that the first 1,000 feet (300 m) of runway 01R, the preferential runway at that time,[7] had also been closed. After consulting with Pan Am flight controllers and the control tower, the crew decided to take off from runway 01R, shorter compared to 28L, with less favorable wind conditions.[8]

Runway 01R was about 8,500 feet (2,600 m) feet long from its displaced threshold (from which point the takeoff was to start) to the end, which was the available takeoff length for Flight 845.[9] Because of various misunderstandings, the flight crew was erroneously informed the available takeoff length from the displaced threshold was 9,500 feet (2,900 m), a thousand feet longer than actually existed. Despite the shorter length, it was later determined that the aircraft could have taken off safely, had the proper procedures been followed.

As the crew prepared for takeoff on the shorter runway, they selected 20 degrees of flaps instead of their originally planned 10 degree setting, but did not recalculate their takeoff reference speeds (V1, Vr and V2), which had been calculated for the lower flap setting, and were thus too high for their actual takeoff configuration.

Consequently these critical speeds were called late and the aircraft's takeoff roll was abnormally prolonged. In fact the first officer called Vr at 160 knots (300 km/h) instead of the planned 164 knots (304 km/h) because the end of the runway was "coming up at a very rapid speed."[10]

Damage

Unable to attain sufficient altitude to clear obstructions at the end of the runway, the aircraft's aft fuselage, landing gear and other structures were damaged as it struck components of the Approach Lighting System at over 160 knots (300 km/h). Three lengths of angle iron up to 17 ft long (5.2 m) penetrated the cabin, injuring two passengers. The right main under-body landing gear was forced up and into the fuselage, and the left under-body landing gear was ripped loose and remained dangling beneath the aircraft. Other systems damaged in the impact included Nos 1, 3 and 4 hydraulic systems, several wing and empennage control surfaces and their mechanisms, electrical systems including the antiskid control, and three of the evacuation slides.

The flight proceeded out over the Pacific Ocean for 1 hour and 42 minutes to dump fuel in order to reduce weight for an emergency landing. During this time, damage to the aircraft was assessed and the injured treated by doctors on the passenger list. After dumping fuel, the aircraft returned to the airport. Emergency services were deployed and the plane landed on runway 28R. During landing, six tires on the under-wing landing gear failed. Reverse thrust functioned only on engine 4, so the aircraft slowly veered to the right, off the runway and came to a stop. There was no fire, though videotape of the landing showed brief flames from the area of the left under-wing landing gear. After stopping, the aircraft slowly tilted backwards due to the missing body gear, which had been ripped off or disabled on takeoff. The aircraft came to rest on its tail with its nose elevated. It was not known that the 747 would tilt backwards without the support of the main body gear, until this accident.

Injuries

There were no fatalities among the 218 passengers and crew aboard, but two passengers were seriously injured during the impact, and during the subsequent emergency evacuation twenty-seven more sustained injuries, eight of them serious.

Rods of angle iron from the ALS structure penetrated the passenger compartment, injuring passengers in seats 47G (near amputation of left leg below the knee) and 48G (severe laceration and crushing of left upper arm).

After landing, the aircraft veered off the runway on its damaged landing gear and came to a halt. Evacuation commenced from the front due to a failure to broadcast the evacuation order over the cabin address system (it was erroneously broadcast over the radio), the order being given by one of the flight crew exiting the cockpit and noticing that evacuation had not commenced. During this time, the aircraft settled aft, resting on its tail in a nose-up attitude. The four forward slides were unsafe for use due to the greater elevation and high winds. Most passengers evacuated from the rear six slides. Eight passengers using the forward slides sustained serious back injuries and were hospitalised. Other passengers suffered minor injuries such as abrasions and sprains.

Investigation

The accident was investigated by the National Transportation Safety Board (NTSB), which issued its final report on May 24, 1972. According to the NTSB, the Probable Cause of the accident was:[2]

...the pilot’s use of incorrect takeoff reference speeds. This resulted from a series of irregularities involving: (1) the collection and dissemination of airport information; (2) aircraft dispatching; and (3) crew management and discipline; which collectively rendered ineffective the air carrier’s operational control system.

Aftermath

Subsequent to the accident, the aircraft was repaired and returned to service. N747PA was re-registered and leased to Air Zaire as N747QC from 1973 until March 1975, when returned to Pan Am, where it was renamed Clipper Sea Lark, and then Clipper Juan T. Trippe in honor of the airline's founder.[3] It remained with Pan Am until the airline ceased operations in 1991, and was transferred to Aerolíneas Argentinas, then briefly to Kabo Air of Nigeria, back to Aerolíneas, and was finally scrapped in 1999 in San Bernardino, California. The aircraft served as a restaurant in Hopyeong, Namyangju, South Korea for some time, until the restaurant closed down. The aircraft was scrapped for good in 2010. [11][12][13]

See also

References

  1. ^ a b c d e "NTSB final report". NTSB. http://www.airdisaster.com/reports/ntsb/AAR72-17.pdf. Retrieved 2009-06-30. 
  2. ^ a b "ASN accident record". Aviation Safety Network. http://aviation-safety.net/database/record.php?id=19710730-2. Retrieved 2009-06-30. 
  3. ^ a b Thompson, Nigel (editor); Ricky-Dene Halliday (co-editor) (1984). Airliner Production List 1984/85. London: Aviation Data Centre. p. 231. ISBN 0946141096. 
  4. ^ "Boeing 747 complete production list". airfleets.net. http://www.airfleets.net/listing/b747-1.htm. Retrieved 2009-06-30. 
  5. ^ Comparing the 1971 runway orientations and lengths described in the NTSB report to the modern ones, only runway 28R has been significantly changed. (See p. 10, NTSB report.)
  6. ^ Crews were repairing a crack which appeared in the pavement that morning.
  7. ^ Due to noise abatement.
  8. ^ Runway 28L was 10,600 feet (3,200 m) long, and the wind was from the west at 22 knots (41 km/h). (See NTSB report, p. 10.)
  9. ^ Boeing 747 aircraft were not authorized to apply takeoff thrust before reaching the displaced threshold of runway 01R, to reduce jetblast effects on a nearby highway (see NTSB report).
  10. ^ The most critical reference speed is Vr, which is when the pilot flying (pilot manipulating the controls, in this flight the captain) "rotates" (lifts the aircraft's nose); if rotation is done too late in the takeoff roll, the climb will be delayed and obstruction clearance reduced.
  11. ^ "Aeroposta N747PA (ex N747QC)". Airfleets. http://www.airfleets.net/ficheapp/plane-b747-19639.htm. 
  12. ^ "Picture of the Boeing 747-121 aircraft". Airliners.net. http://www.airliners.net/photo/Boeing-747-121/1471902/&sid=bedfade942d0fe487f6c505821469f3f. Retrieved 2009-06-30. 
  13. ^ "N747PA rusting away". PPRuNe. https://www.pprune.org/jet-blast/370996-n747pa-rusting-away.html. Retrieved 2009-06-30. 

External links